Tuesday, May 21, 2019

1017 Boeing outsourced. Substandard parts, made in China with non-aerospace material, installed in 777 and 737

Boeing outsourced. Substandard parts, made in China with non-aerospace
material, installed in 777 and 737

Newsletter published on May 15, 2019

(1) Whistleblower on FAA, Boeing and Moog Aircraft cover-up of a Boeing
safety threat
(2) Some Boeing Jets Have Substandard Parts, Whistleblower Claims
(3) Inspector General Says FAA Not Doing Enough to Stop Bogus Parts from
Getting on Commercial Flights
(4) Boeing was told 737 Max had safety flaws in 2017, say unions
(5) Boeing knew about 737 MAX problems for months, but didn't tell FAA
until after 2018 Lion Air crash
(6) On 737 MAX, two toggle switches were altered to perform the same
function

(1) Whistleblower on FAA, Boeing and Moog Aircraft cover-up of a Boeing
safety threat


From: Eric Walberg [mailto:walberg2002@yahoo.com]

hi peteri just got this email from linkedin. you are the expert on this
technical stuff. see if it's of interest.

My name is Charles Shi, I am a whistleblower on the FAA, Boeing and Moog
Aircraft criminal cover-up of a Boeing safety threat. I wonder if you
may do a story on the massive Chinese fake Safety parts of flight
control hardware of B737 including max.While media focus on the MCAS
causing the Max crashes, it is the time to look at the flight control
hardware failure that may be the direct cause of Max Crashes.

Latest breaking story: A Whistleblower Charges Boeing Jets Have
Substandard Parts
https://www.theepochtimes.com/a-whistleblower-charges-boeing-jets-have-substandard-parts_2854171.html

this article did not touch on the FAA inaction..

In last three years, FAA refused repeatedly to refer the matter to law
enforcement for criminal investigation no matter what warning was given.
So far, the threat was not removed due to massive cover up by Moog,
Boeing, FAA and now even by watchdog IG of DOT. Recent FOIA result found
that the FAA removed my whistleblowing case from the total 223 Suspected
Unapproved Parts?SUP? cases between 2014-2018 which is probably the only
exception. Other minor SUP cases were referred to the law enforcement
for criminal investigation.

My own blog;
https://faaoversightextraordinaryairsafetythreat.wordpress.com/2018/07/31/a-matter-of-massive-counterfeiting-boeing-safety-partsI
wish you may do a story on the continued FAA inaction and cover-up. I
shall share an online onenote file with key unredacted exhibits embedded
to your email once your interest is advised.

Thank you!
Please feel free to contact me:
Charles Shi
Cell:+86 17717283030
ZOOM:915-332-7598
Skype: charles20160318
Email: charlesshi88@outlook.com
Youtube:
https://www.youtube.com/playlist?list=PLwjrs24cNrv1CwuFG5ikJZ-k7Zv7mFvrp
Google+: https://plus.google.com/+CharlesShi
Facebook: https://www.facebook.com/charles.shi.925
Weibo: https://weibo.com/u/5339000986?refer_flag=1005055010_&is_all=1

(2) Some Boeing Jets Have Substandard Parts, Whistleblower Claims

https://www.theepochtimes.com/a-whistleblower-charges-boeing-jets-have-substandard-parts_2854171.html

BY JENNIFER ZENG

March 26, 2019 Updated: March 27, 2019

As investigations of the crashes of two Boeing 737 MAX jetliners
continue, a former supply chain manager of the contractor for Boeing’s
flight control systems says that substandard parts made in China with
non-aerospace material have been installed in 777 and 737 planes that
are still in service.

Now, the whistleblower, Charles (Chaosheng) Shi, is intensifying his
efforts to bring light to the issue, which has been troubling him for
three years.

Shi worked for Moog Aircraft for 10 years, from 2006 to 2016. In 2006,
he set up the Moog supply chain in China and almost all suppliers were
audited and approved by him, except for the one he’s now accusing of
providing substandard parts.

He has tried to bring his concerns about the faulty parts to the
attention of Moog, Boeing, the U.S. Federal Aviation Administration
(FAA), U.S. Department of Transportation, the U.S. Congress, and
President Donald Trump. The FAA found that two of Shi’s concerns were
substantiated, while others were not.

He also reported the issue to Chinese authorities, including Chinese
leader Xi Jinping, the Civil Aviation Administration of China, and even
the Shanghai Public Security Bureau.

In an interview with NBC in February 2018, Shi expressed concern that
Boeing parts supplied by Moog were outsourced to a third-party Chinese
supplier that used cut-rate manufacturing processes.

Shi said, "You need to bake the parts to get the hydrogen out of the
parts, so the parts can still be solid with integrity. Otherwise, the
hydrogen goes into the parts. That can make the parts brittle, so the
parts can fail."

He also related to NBC an additional violation that was substantiated by
the FAA, concerning unbaked parts in Boeing 777 spoilers: a hydrogen
embrittlement hazard that might cause the parts and system to fail
during flight.

Shi told The Epoch Times that the parts in question are mainly
components in the Boeing 777 and 737 spoiler systems, which are deployed
during takeoff, early flight, and landing.

Alarming Findings

Shi said he became aware in 2015 that Suzhou New Hongji Precision Parts
Co. (NHJ) in Jiangsu Province, China, one of Moog’s suppliers, was
reportedly using cheap and substandard materials. He confirmed that with
another aviation manufacturer, B/E Aerospace, the sole source for
lavatories on Boeing 737 aircraft built since 2012, and the only other
aerospace customer of NHJ.

B/E Aerospace stopped buying from NHJ in 2013, after it was found that
NHJ faked raw material certificates and used substitute materials,
resulting in B/E product failures, Shi said.

As the manager for Moog Aircraft, Shi said he was responsible for the
quality of the parts and materials that were purchased from all
suppliers, and had the right to audit those suppliers.

Shi later told the FAA that he believed, based on his investigation,
that NHJ had faked the raw material purchase record, and outsourced
parts for Moog to an unknown supplier.

"NHJ was outsourcing Moog/Boeing business to other unknown and
unapproved sub-contractors. One-third of Moog’s business, which was
Boeing plane parts, was outsourced to illicit sub-contractors during
2015-2017. And I am willing to testify to this under oath," Shi told The
Epoch Times.

FAA Investigation

Shi’s discovery of the outsourcing was confirmed by an FAA investigation
conducted in September 2016. According to an FAA memorandum, obtained
through a Freedom of Information Act request, two allegations made by
Shi were found "substantiated":

"Moog’s supplier NHJ outsourced Moog machined parts to an unknown
supplier. "Shenhai, a NHJ subcontractor, did not properly bake parts
both before and after the cadmium plating process, and forged the
production process card. The improperly baked parts consisted of four
different part numbers."

However, Shi’s seven other allegations were found "not substantiated" by
the same investigation.

According to the FAA memorandum, "Moog auditors identified the following
nonconformance issues:

"(a) Required stress relief (baking) was not performed prior to cadmium
plating;

"(b) Hydrogen embrittlement relief treatment (baking) after cadmium
plating was performed for only 4 hours on all parts, not 8 hours as
required per AMS-QQ-P-416C specification;

"(c) Baking procedure controls were not per AMS2750 specification; and

"(d) No records of furnace traces [times] were being maintained for more
than one week."

The FAA investigation also confirmed that "273 discrepant parts
delivered to Boeing were installed into spoilers on the Boeing 777
aircraft."

Safety Critical

Of greatest concern to Shi is that many NHJ parts are "safety
sensitive," and one is "safety critical."

One part (Part number: P665A0039–02) is the blocking or mounting lug of
the Boeing 737’s spoiler. This is a "Single Point Of Failure (SPOF)"
part; if this part fails, the entire system will fail, which may cause a
fatal accident.

According to a purchase list provided by Shi, Moog has bought 6986 SPOF
parts from NHJ during 2015-2017. Shi said these parts can be used to
equip more than 600 aircraft, as each 737 uses 10 pieces.

Shi said Moog is the exclusive supplier for all models of the Boeing
737, including the Max planes, and NHJ is the only supplier for this
SPOF part for the 737 spoiler. His conservative estimate is that 500
Boeing planes may have been compromised, and are still in service.

When contacted by the Epoch Times, Moog denied Shi’s allegations with
this one-sentence statement: "In response to your request, please note
that the Moog parts Mr. Shi references are not on the 737 MAX."

The Epoch Times submitted a follow-up inquiry to Moog, with a list of 58
different NHJ parts purchased by Moog, and asked Moog to clarify and
verify on which planes these parts are used.

Moog hasn’t responded to the request.

Shi said, "The motive of NHJ’s using substitute material was that the
substitute material was one-third or even one-half cheaper."

NHJ couldn’t be reached for comment.

‘Serious Safety Threat’

Shi said he first became concerned about the parts in May 2015, when two
of his supplier development engineers told him that NHJ had a bad
history and B/E Aerospace stopped using the company. He became worried
and reported that to his direct supervisor. But his supervisor, who had
brought in NHJ as a supplier for Moog, brushed it off.

Shi also conducted some auditing and investigative work, finding that
NHJ was using an "illicit material booking MID system (Material
Identification)," which violated aerospace industry standards. NHJ MID
numbers had no traceability to raw material sourced from approved raw
material vendors.

"This violation is totally not acceptable," Shi said.

Shi also traveled to NHJ a few times after the discovery of the faulty
recordkeeping, and found that NHJ stocked raw material for Moog in an
open area. That material was mixed with other supplies and was
improperly labeled, he said. Some material was labeled; some was not.

Shi also found that some "work in process" paperwork didn’t have MID
"traceability," which means that NHJ had no traceability in its
manufacturing process.

On Aug. 7, 2015, Shi became a whistleblower within his company, by
bringing the issue to global supply chain management of Moog Aircraft.

Shi said he later found that NHJ used faked certificates to fabricate
quantities of products they purchased from an approved vendor. He said
he was able to determine that from a document he obtained from the
approved vendor, showing the quantity of how many units it sold to NHJ,
which was only one-third of what NHJ claimed that they had bought.

On Jan. 12, 2016, Shi alerted the president of Moog Aircraft and the CEO
of Moog Inc., the parent of Moog Aircraft, about the "alarming safety
threat." The next day, Shi took the matter to the U.S. FAA. That was
also the day he was fired.

According to Reuters, Moog said Shi’s employment was ended as part of a
"previously communicated global reorganization," and wasn’t related to
him raising issues about the supplier’s quality.

According to the FAA memorandum, after receiving Shi’s report, the FAA
investigator visited the Moog plant in East Aurora, New York, on March
29, 2016, and interviewed Moog employees "who were most familiar with
the process." After reviewing materials provided by Moog, and witnessing
"retesting of the materials properties of parts," the FAA concluded that
Shi’s allegation was "not substantiated."

In August 2016, Shi provided what he describes as additional
"compelling" evidence to the FAA. He told the agency about NHJ faking
documents about SPOF parts, which were used in the Boeing 737 spoiler,
and requested that the FAA reopen the case.

The FAA did another round of investigation and found two items out of
Shi’s nine allegations were "substantiated."

According to the FAA, in response to the substantiated allegation that
NHJ had provided improperly manufactured parts, Moog’s product
engineering team chose six parts from the suspect lots and "subjected
them to high sustained stress load testing." There were "no noted
failures." Moog recommended "use as is" for the parts that had already
been installed on Boeing planes, which Boeing accepted.

Regarding Shi’s claim that NHJ had faked its record of purchases of raw
materials, the FAA reports that Moog discovered an "accounting error"
that resulted in the discrepancy, which resulted in the agency
determining this allegation wasn’t substantiated.

Shi says he’s not satisfied with FAA’s handling of the matter,
especially the substantiated allegations. He found himself "to be in
disbelief that the FAA decided to let these admittedly unauthorized and
literally unbaked parts to remain in service, sparing Moog and/or Boeing
millions of dollars for removal and retrofitting."

In response to the Epoch Times’ request for information and comment
regarding Shi’s allegations, the FAA emailed the following statement:

"The FAA closed its Moog investigation regarding Mr. Shi’s allegations.
The agency determined the corrective action defined by Moog and Boeing
associated with the open substantiated allegation was appropriate to
address the related issues identified in the investigation. The FAA
investigation determined unsafe conditions did not exist."

Boeing hasn’t responded to requests for comment.

A Late-Night Intrusion

Shi says his allegations that NHJ faked documents and used inferior
materials should be referred to criminal investigators, which he said he
has repeatedly asked the FAA to do.

After the recent Boeing 737 Max crashes, he has stepped up his efforts
by writing to U.S. Rep. Peter DeFazio (D-Ore.) and Rep. Brian Mast
(R-Fla.), as well as President Trump. He said he’s willing to travel to
the United States at his own cost to testify to Congress, should
Congress decide to hold a hearing on this.

Shi has also taken to social media and Change.org to expose the issues
and to draw public attention. He hopes more mainstream media can take up
his story.

Shi said his home in Shanghai was entered in a disturbing manner on
March 13.

"It was the security guard who told me my doors were open. I went down
to check two doors, one was the courtyard entrance door in the north,
one was the door to my townhouse in the south. Both were wide open. I
called police and the fact was recorded by policemen who rushed to my
home. The doors were intact but wide open. Nothing got lost. All things
were in a tidy state."

Shi believes that incident was a warning, with the intruders
demonstrating how easily they could reach him. They want him, he said,
to stop his efforts to expose the problems with NHJ’s parts.

(3) Inspector General Says FAA Not Doing Enough to Stop Bogus Parts from
Getting on Commercial Flights


https://www.nbcbayarea.com/investigations/FAAs-Inspector-General-Says-Agency-Not-Doing-Enough-to-Stop-Bogus-Parts-from-Getting-on-Commercial-Flights-475352673.html

By Stephen Stock, Michael Horn and Kevin Nious

Published Feb 27, 2018 at 10:44 PM | Updated at 9:52 AM PST on Feb 28, 2018

The Department of Transportation's Inspector General says the "FAA’s
oversight of industry actions to remove unapproved parts (from the
nation’s aviation system) is ineffective," and the agency "cannot be
assured that unapproved parts … no longer pose a threat to safety" for
the traveling public.

That OIG report has prompted ranking member of the U.S. House
Transportation and Infrastructure Committee, Rep. Peter DeFazio,
(D-Oregon), to vow to crack down on unapproved airplane parts that he
says pose a safety risk to the flying public. The inspector general’s
report echoes a series of stories by NBC Bay Area’s Investigative Unit
that first aired in 2016. The Investigative Unit’s reporting found
thousands of unapproved parts made their way onto and into the systems
of commercial aircrafts.

NBC Bay Area also found aviation suppliers and manufacturers who
continued to sell unapproved parts even after receiving FAA sanctions.

"We really need to pay a lot more attention to this. How parts are
manufactured and tracked throughout their life and ultimately destroyed
at the end so they can’t be snuck back into the part stream," DeFazio
told NBC Bay Area.

Concerned about the FAA’s oversight or lack thereof, DeFazio was the one
who asked the Inspector General’s Office to audit the FAA’s suspected
unapproved parts program.

"I don’t understand what’s going on at the FAA. I asked for that report
to see if we have made progress in the last 20 years, and it appears
that very little has been made," DeFazio said. "One critical component
that isn’t up to manufacturer’s standards could take down a plane mid-air."

The audit criticized the FAA for a lack of recordkeeping, management
control, and inaccuracies in tracking unapproved parts.

For these reasons, FAA cannot be assured that unapproved parts have been
removed from the system and no longer pose a threat to safety.DOT OIG

CHINESE PARTS ON AMERICAN PLANES

Officials at the Inspector General's Office aren't the only ones raising
safety concerns about unapproved parts ending up in commercial airplane
systems. Industry whistleblower Charles Shi, who worked for an aviation
parts supplier for Boeing aircraft, believes the problem of unapproved
parts is worse than the FAA acknowledges.

Shi worked as a quality control inspector based in China, overseeing
parts made for Boeing aircraft.

During his inspections, Shi says he found that parts outsourced to
another third party Chinese supplier were made with inferior materials
that were not "baked" long enough to harden appropriately during production.

"You need to bake the parts to get the hydrogen out of the parts. So the
parts can still be solid with integrity. Otherwise the hydrogen goes
into the parts that can make the parts thin and brittle so the parts can
fail," Shi told NBC Bay Area.

The parts in question are components in a Boeing 777’s spoiler system,
which allows an airplane to take off and land safely.

Shi took his safety concerns to the FAA. According to documents from an
FAA whistleblower investigation,  officials confirmed that hundreds of
parts used on Boeing 777’s were manufactured in violation of FAA
standards and that documents were "fabricated" by a third party Chinese
supplier to conceal the violation. Even so, the FAA still allowed Boeing
to install the parts "as is." Those parts remain on Boeing aircraft to
this day.

On March 14, 2016 Charles Shi filed a whistleblower complaint with the
FAA alleging substandard materials and processes were used by a Chinese
manufacturer to produce parts intended for Boeing aircraft.

A spokesperson for Shi’s former employer, Moog Inc., said the parts in
question were tested and determined to meet specifications. "There have
been no reported issues with these parts. The FAA investigated and
determined all necessary corrective actions had been taken," the
spokesman said.

A spokesperson for Boeing said the company also found no issues with the
parts in question, stating:

"The safety of the flying public is Boeing’s primary concern, and any
allegation related to safety is thoroughly investigated. In late 2016,
the U.S. Federal Aviation Administration investigated allegations
related to suppliers to Moog. Boeing cooperated fully. The FAA
investigations, as well as Boeing and Moog, found no evidence of a
safety risk related to these allegations. Any claim otherwise is false."

"A lot of our airlines have outsourced their heavy maintenance to
overseas where, you know, one criminal could put in a part that's going
to cause a critical failure in that plane. One terrorist could put in a
part that intentionally is going to fail," DeFazio said.

FAA records analyzed by the Investigative Unit revealed incidents like
these happen more often than the public is aware. Investigation reports
and unapproved part notifications found more than 2,800 individual
airplanes that had unapproved parts discovered on them since 2011,
including on U.S. commercial air carriers.

California Company Continued to Sell Bogus Aircraft Parts Despite FAA
Cease-and-Desist OrderCalifornia Company Continued to Sell Bogus
Aircraft Parts Despite FAA Cease-and-Desist Order

The NBC Bay Area Investigative Unit found thousands of instances where
bogus and potentially dangerous airplane parts were surreptitiously
installed on planes including major commercial airliners. The Federal
Aviation Administration sanctions repair shops and manufacturers who
deal bogus parts, but records show that doesn’t always stop some
compani... Read more(Published Thursday, May 18, 2017) Former Acting FAA
Administrator Joseph Del Balzo believes the agency could do more to root
out bogus parts from the industry.

"I don't think anybody really knows how serious the issue really is,"
Del Balzo told NBC Bay Area. Through his firm, JDA Aviation Technology
Solutions, Del Balzo helps train inspectors how to identify bogus parts.
"The FAA certainly doesn’t have the resources to go out and get the
data. ... I don't think anybody knows how serious the issue really is."

FAA ENFORCEMENT

FAA Acting Administrator Daniel K. Elwell told the Investigative Unit
his agency is reviewing the inspector general’s recommendations while
also touting his agency’s safety track record.

"There has not been a commercial passenger fatality in the U.S. in nine
years. It's an amazing safety record that is borne from a collaborative
approach to safety," Elwell said.

As a former commercial pilot, Elwell said he does not believe unapproved
parts pose a safety risk to the flying public.

"I've been flying for longer than I care to admit and was recently
checked out again. So if I had a concern about it, I wouldn't be
flying," Elwell told NBC Bay Area.

Meanwhile, DeFazio said he is working to strengthen regulations that
would allow investigators to more easily identify legitimate aviation parts.

"I want to see every part indelibly marked at the manufacturer, tracked
throughout its lifespan and disposed of properly at the end of its
lifespan."

If you have a tip for the Investigative Unit, give us a call at
1-888-996-8477, or you can reach us via email at TheUnit@nbcbayarea.com

(4) Boeing was told 737 Max had safety flaws in 2017, say unions

https://www.smh.com.au/business/companies/boeing-was-told-737-max-had-safety-flaws-in-2017-say-unions-20190515-p51neb.html

May 15, 2019 — 6.01am

Three unions representing aviation safety inspectors said in a sharply
worded report months before the Boeing's 737 Max was approved for use
that the planemaker was given too much authority to oversee itself and
that the new jet had safety flaws.

The new version of the decades-old 737 was approved with a vulnerable
flight-control system and flaws in its fuel tank because Boeing and
Federal Aviation Administration management overruled front-line workers,
the report charged.

The report, obtained by Bloomberg News, didn't raise concerns about a
safety feature implicated in two crashes since October that killed a
total of 346 people. There's no indication the issues identified by the
unions led to incidents. Boeing said in a statement that the plane was
certified "in full accordance" with FAA procedures.

But the report took aim at a controversial FAA program encouraged by
Congress that gave manufacturers such as Boeing more authority to
approve their own designs. The agency wanted to transition its workforce
of engineers, pilots and inspectors who assess new aircraft designs to
focus on only the highest risk issues and on auditing the work of companies.

"The unions are concerned that the safety benefits of a second set of
eyes provided by direct oversight of both domestic and foreign
certification projects in high risk aspects of the certification process
has not been recognised as an essential function within" FAA, the unions
wrote in the report.

Leaders of the FAA and the National Transportation Safety Board, which
is assisting in investigations of the crashes, are scheduled to testify
Wednesday before a House aviation hearing.

While the FAA itself signed off on at least the preliminary design of
the Manoeuvering Characteristics Augmentation System or MCAS, which was
driving down the noses of the two planes that crashed, some of the
approvals were granted by Boeing employees designated to act as
representatives of the FAA.

These so-called designees have become a lightning rod in the aftermath
of the crash on October 29 of a Lion Air 737 Max off the coast of
Indonesia and an Ethiopian Airlines jet on March 10. In both cases, the
MCAS system was repeatedly trying to push the plane into a dive. Neither
crew managed to counteract the system and each eventually crashed.

The 737 Max, Boeing's best-selling aircraft, has been grounded since
March 13 as the manufacturer works on new software to address the accidents.

One of the areas under investigation following the accidents is how the
FAA and Boeing categorised the risks of an MCAS failure. A malfunction
of the system was deemed to be "major" or the more serious
classification "hazardous," depending on when it occurred during flight,
according to the FAA.

MCAS was not categorised as "catastrophic," the most severe condition
that requires additional layers of protection. That classification is
reserved for failures that can't be countered by pilot actions and would
lead to multiple fatalities.

Current and former FAA officials say that the process of using
designated representatives of manufacturers isn't inherently unsafe so
long as its properly overseen. The FAA would have to hire 10,000 more
employees and increase its budget by $US1.8 billion ($2.6 billion) if it
didn't rely on company employees, acting Administrator Daniel Elwell
testified at a Senate hearing in March.

FAA unions oppose expanding the program because they say it gives too
much authority to companies and that employees have an incentive to side
with their bosses. While unions didn't cite employment issues in their
report, decreasing the role of company representatives could lead to
more FAA jobs.

The three unions - National Air Traffic Controllers Association,
Professional Aviation Safety Specialists and American Federation of
State, County and Municipal Employees - wrote that designees had failed
to address safety issues on multiple aircraft models. Portions of the
report were earlier cited by the Seattle Times.

Among the issues the unions identified on the 737 Max, which was nearing
certification in early 2017, was a rudder control system that lacked
adequate redundancy, a refueling system that could lead to spills and
fuel tank wiring.

The FAA investigated the issues after the union filed the report, it
said in a statement. The agency declined to say what steps, if any, it
took in 2017 to address the specific allegations because of the numerous
investigations currently underway into the plane. In addition to reviews
by FAA committees, Congress and the Transportation Department, the
Justice Department is conducting a criminal probe of how the plane was
certified.

The FAA has defended the certification process for the 737 Max, saying
it was done according to long-standing practice.

Boeing has reported no new orders for its 737 MAX after its worldwide
grounding, as well as disappointing orders and deliveries for the entire
quarter.

All the issues identified by the union involved features on older
versions of the plane that wouldn't be permitted if the company was
developing a model from scratch. When manufacturers such as Boeing
update an existing model, the FAA has leeway to approve such designs if
it finds that safety isn't compromised.

The growing use of designated employees to assist in certification is
part of the evolving philosophy of greater cooperation between the FAA
and the companies it regulates, Boeing said in a statement.

"The long-standing collaborative engagement between the FAA, Boeing, its
customers and industry partners has created the safest transportation
system in the world," the company said.

The 737 Next Gen models that preceded the Max family have one of the
lowest accident rates of any modern jetliners, according to Boeing's
annual accident summary.

Bloomberg

(5) Boeing knew about 737 MAX problems for months, but didn't tell FAA
until after 2018 Lion Air crash


https://www.abc.net.au/news/2019-05-06/boeing-knew-737-problems-before-lion-air-ethiopia-crashes/11084326

Updated 6 May 2019, 9:29pm

Boeing has admitted it discovered a safety alert in the cockpit of its
737 MAX plane was not working as intended, yet it did not disclose that
fact to airlines or US federal regulators until after one of the planes
crashed months later.

Key points:

- Boeing realised its 737 model's sensor warning light only worked when
an additional feature was bought within months of its 2017 debut

- The FAA said it was first notified of the issue in November 2018,
after the Lion Air crash

- It is not clear whether purchase of the additional feature would have
prevented crashes in Indonesia or Ethiopia

- The feature was designed to warn pilots when a key sensor might be
providing incorrect information about the pitch of the plane's nose.

But within months of the 737's debut in 2017, Boeing said, its engineers
realised the sensor warning light only worked when airlines also bought
a separate, optional feature.

The sensors malfunctioned during an October flight in Indonesia and
another in March in Ethiopia, causing software on the planes to push
their noses down.

Pilots were unable to regain control of either plane, and both crashed,
killing 346 people total.

It is not clear whether having the warning light would have prevented
either the Lion Air crash or the crash of an Ethiopian Airlines MAX near
Addis Ababa.

The crash was the worst airline disaster in Indonesia in more than two
decades.

Boeing's disclosure on Sunday (local time), however, raised fresh
questions about the company's candour with regulators and airline customers.

Boeing said again that the plane was safe to fly without the sensor
alert, called an angle-of-attack disagree light.

Other gauges tell pilots enough about the plane's speed, altitude,
engine performance and other factors to fly safely, the company added.

A spokesman for the US Federal Aviation Administration (FAA) said the
agency was first notified of the non-working warning light in November,
after the Lion Air 737 MAX crashed in Indonesia.

He said FAA experts determined that the non-working cockpit indicator
presented a low risk.

"However, Boeing's timely or earlier communication with [airlines] would
have helped to reduce or eliminate possible confusion," the spokesman
said in a emailed statement emailed to Associated Press.

He declined to give more details.

In manuals that Boeing gave to Southwest Airlines — the biggest operator
of both the MAX and 737s in general — the warning light was depicted as
a standard feature just as it is on older 737s, according to Southwest
spokeswoman Brandy King.

After the Lion Air crash, Ms King said, Boeing notified Southwest that
it had discovered the lights did not work without the optional
angle-of-attack indicators, so Southwest began adding the optional
feature too.

That allowed the airline to activate the sensor-disagree warning lights
on its 34 MAX jets earlier this year, she said.

Ms King described both features as "supplemental" and "advisory" to
other information provided to pilots during flights.

The indicator was designed to tell pilots when sensors that measure the
pitch of the plane's nose appeared to conflict, a sign that the sensor
information is unreliable.

Boeing told airlines that the warning light was standard equipment on
all MAX jets.

Boeing engineers quickly learned, however, that the warning light only
worked if airlines also bought an optional gauge that told pilots how
the plane's nose was aimed in relation to the onrushing air.

Boeing said the problem stemmed from software delivered to the company.

A Boeing spokesman declined to name the software vendor to Associated Press.

In its statement on Sunday, Boeing said that because in-house experts
decided that the non-working light did not affect safety, the company
decided to fix the problem by disconnecting the alert from the optional
indicators at the next planned update of cockpit display software.

Boeing did not tell airlines or the FAA about this decision.

Moving forward, Boeing said it hoped to win approval from the FAA and
foreign regulators to get the MAX flying again before summer in the
northern hemisphere is over.

When it does, the company said, the sensor warning light will be standard.

Nearly 400 MAX jets were grounded by airlines worldwide in mid-March
after the Ethiopia crash.

Boeing was working to fix the software that pitched the planes' noses
down based on faulty sensor readings, and to provide pilots with more
information about the plane's automation.

Meanwhile, the US Justice Department was conducting a criminal
investigation into whether Boeing misled regulators about features on
the plane including flight-control software at the heart of the crash
investigations.

The company was also under scrutiny by congressional committees and the
Transportation Department's inspector general, and it faces a growing
number of lawsuits by families of the dead passengers.

AP

(6) On 737 MAX, two toggle switches were altered to perform the same
function


https://www.zerohedge.com/news/2019-05-11/boeing-dangerously-altered-mcas-toggle-switches-737-max-deadly-crashes

by Tyler Durden

Sat, 05/11/2019 - 11:30

When Boeing transitioned from the 737 NG model to the 737 MAX, designers
altered a toggle switch panel that could have prevented both of the
deadly crashes over the last year in Ethiopia and Indonesia, killing a
combined 346 people, according to an investigation by the Seattle Times.

On the 737 NG, the right switch was labeled "AUTO PILOT" - and allowed
pilots to deactivate the plane's automated stabilizer controls, such as
the Maneuvering Characteristics Augmentation System (MCAS), suspected to
be the culprit in both crashes. The left toggle switch on the NG would
deactivate the buttons on the yoke which pilots regularly use to control
the horizontal stabilizer.

On the 737 MAX, however, the two switches were altered to perform the
same function, according to internal documents reviewed by the Times, so
that they would disable all electronic stabilizer controls - including
the MCAS and the thumb buttons on the yoke used to control the
stabilizer. (Dimas Ardian / Bloomberg)

Former Boeing flight-controls engineer Peter Lemme, a harsh critic of
the MAX design, first raised questions over the switch alteration on his
blog, and says he doesn't understand why Boeing made the change.

He said if the company had maintained the switch design from the 737 NG,
Boeing could have instructed pilots after the Lion Air crash last year
to simply flip the "AUTO PILOT" switch to deactivate MCAS and continue
flying with the normal trim buttons on the control wheel. He said that
would have saved the Ethiopian Airlines plane and the 157 people on board.

"There’s no doubt in my mind that they would have been fine," Lemme
said. -Seattle Times

Boeing told the Times that they had historically called for pilots to
flip both switches to disable a problematic or "runaway" stabilizer, so
the button change matched that procedure, adding that the two switches
"were retained for commonality of the crew interface."

"Boeing strongly disagrees with any speculation or suggestion that
pilots should deviate from these long-established and trained safety
procedures," the company added.

During the October Lion Air flight, pilots were reportedly unaware of
the MCAS system - while the day before, an off-duty pilot with knowledge
of the stabilizer controls helped pilots disable the system on the same
plane. Data from the flight revealed that the repeated commands from the
MCAS system sent the flight from Bali to Jakarta plummeting into the sea.

After that crash, Boeing issued a directive calling for pilots to use
the typical runaway stabilizer procedure to deal with MCAS in the event
of a problem. Then pilots would be able to swivel the tail down manually
by physically turning a control wheel that connects to the tail via cables.

But on the Ethiopian Airlines flight, the pilots appear to have
recognized the errant MCAS problem and flipped the cutoff switches as
described in the checklist. But then it appears that the pilots were
unable to move the manual wheel, likely because the forces on the tail
made it physically challenging to turn. -Seattle Times

After they were able to manually control the stabilizer, the Ethiopian
Airlines pilots appear to have flipped the cutoff switches back on,
reactivating the MCAS system. Shortly after, it entered a fatal nosedive
which killed all 157 people aboard.

"When you’re pulling on the column with 80-100 pounds of force trying to
save your life, your troubleshooting techniques are very weak," said
aviation consultant Doug Moss. "You need some gut-level instinctive
things to do to solve the problem."

A veteran Boeing 737 test pilot said that all Boeing planes have two
such cutoff switches, not just the 737. And both he and American
Airlines Captain Dennis Tajer, a spokesman for the Allied Pilots
Association who flies 737s, said they could think of no existing
procedure that called for flipping only one of the switches.

The procedure appears to be designed to prepare for a situation in which
the plane’s stabilizer motor is for some reason jammed and moving
uncommanded in one direction – a classic "runaway stabilizer" situation.
That would require shutting off all power to the motor. -Seattle Times

Notably, the FAA did not notify pilots that the functionality of the
switches had been altered, simply noting in its documentation the
labeling change "Stab Trim cutout switches panel nomenclature."

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